[1]熊小京,冯喆文.垃圾渗滤液厌氧BF/好氧MBR工艺的脱氮特性[J].华侨大学学报(自然科学版),2008,29(1):68-71.[doi:10.11830/ISSN.1000-5013.2008.01.0068]
 XIONG Xiao-jing,FENG Zhe-wen.Study on Nitrogen Removal Behavior in Landfill Leachate Treatment by a Combination of Anaerobic Bio-Filter and Aerobic Membrane Bioreactor Process[J].Journal of Huaqiao University(Natural Science),2008,29(1):68-71.[doi:10.11830/ISSN.1000-5013.2008.01.0068]
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垃圾渗滤液厌氧BF/好氧MBR工艺的脱氮特性()
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《华侨大学学报(自然科学版)》[ISSN:1000-5013/CN:35-1079/N]

卷:
第29卷
期数:
2008年第1期
页码:
68-71
栏目:
出版日期:
2008-01-20

文章信息/Info

Title:
Study on Nitrogen Removal Behavior in Landfill Leachate Treatment by a Combination of Anaerobic Bio-Filter and Aerobic Membrane Bioreactor Process
文章编号:
1000-5013(2008)01-0068-04
作者:
熊小京冯喆文
厦门大学环境科学研究中心; 厦门大学环境科学研究中心 福建厦门361005; 福建厦门361005
Author(s):
XIONG Xiao-jing FENG Zhe-wen
Environmental Science Research Center, Xiamen University, Xiamen 361005, China
关键词:
垃圾渗滤液 厌氧生物滤池 好氧膜生物反应器 硝化 反硝化
Keywords:
landfill leachate anaerobic bio-filter aerobic membrane bioreactor nitrification de-nitrification
分类号:
X703
DOI:
10.11830/ISSN.1000-5013.2008.01.0068
文献标志码:
A
摘要:
采用厌氧生物滤池(BF)与好氧膜生物反应器(MBR)组合工艺,以实际垃圾渗滤液为处理对象,在连续进水条件下,考察该工艺在处理垃圾渗滤液时,进水稀释倍率、厌氧/好氧(A/O)回流比和C/N比值对其硝化与反硝化特性的影响.结果表明,在处理稀释10倍的渗滤液时,氨氮和总氮的平均去除率分别稳定在90%和65%附近,回流比和C/N比值对好氧的硝化与厌氧反硝化反应的影响很小; 在处理稀释5倍的渗滤液时,提高C/N比值能使厌氧反硝化能力增强,有效地消除亚硝氮的积累.渗滤液中有较高的浓度的氨氮与有机物负荷,容易对硝酸化菌产生抑制作用,使膜出水的亚硝氮积累明显,氨氮和总氮平均去除率分别稳定在69%~78%和46%~50%.
Abstract:
The nitrogen removal behaviors in landfill leachate treatment were investigated under various dilution ratios,recycle ratios and C/N using a combination of anaerobic bio-filter(BF) and aerobic membrane bioreactor(MBR) process.The results showed that when dilution ratio of landfill leachate was set at 10,the average removal efficiency of NH+4-N and TN possibly reached at about 90% and 65%,respectively.Both nitrification and de-nitrification activities in anaerobic bio-filter and aerobic MBR were not affected under the various recycle ratios and C/N.However,when dilution ratio dropped to 5,although the de-nitrification activity could be enhanced effectively and nitrite accumulation was eliminated by increasing the C/N.But due to the relatively high strength of ammonia and organic compound containing in influent,the activity of nitrifying bacteria in aerobic MBR was easily inhibited and nitrite was accumulated significantly,which led to the average removal efficiencies for both NH+4-N and total N in whole system could be maintained at the range of 69%~78% and 46%~50%,respectively.

参考文献/References:

[1] 赵庆良, 李湘中. 垃圾渗滤液中的氨氮对微生物活性的抑制作用 [J]. 环境污染与防治, 1998(6):1-4.
[2] 王宝贞, 王承武, 杨铨大. A(缺氧活性污泥)/B(A/O淹没式生物膜)复合系统处理垃圾填埋场渗沥液 [J]. 给水排水, 1996(5):15-18.
[3] 申欢, 金奇庭, 李明波. 膜生物法处理城市垃圾渗滤液 [J]. 中国给水排水, 2004(3):56-59.doi:10.3321/j.issn:1000-4602.2004.03.016.
[4] 任鹤云, 李月中. MBR法处理垃圾渗滤液工程实例 [J]. 给水排水, 2004, (10):36-38.doi:10.3969/j.issn.1002-8471.2004.10.011.
[5] 陈忠. 垃圾渗沥液A/O生化-PW生物膜处理技术 [J]. 有色冶金设计与研究, 2001(4):58-60.doi:10.3969/j.issn.1004-4345.2001.04.014.
[6] 熊小京, 简海霞. A/O MBR与BAF组合工艺处理垃圾渗滤液 [J]. 工业水处理, 2007(9):39-42.doi:10.3969/j.issn.1005-829X.2007.09.011.
[7] 林燕, 何义亮, 孔海南. MBR中同步硝化反硝化及异养硝化现象试验研究 [J]. 膜科学与技术, 2006(2):22-26.doi:10.3969/j.issn.1007-8924.2006.02.006.

相似文献/References:

[1]林建清,方宏达,杨春霖,等.厌氧氨氧化去除垃圾渗滤液中氨氮的实验[J].华侨大学学报(自然科学版),2008,29(1):61.[doi:10.11830/ISSN.1000-5013.2008.01.0061]
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备注/Memo

备注/Memo:
福建省自然科学基金计划资助项目(D0610021)
更新日期/Last Update: 2014-03-23